ISSN: ISSN 2472-0518

石油とガスの研究

オープンアクセス

当社グループは 3,000 以上の世界的なカンファレンスシリーズ 米国、ヨーロッパ、世界中で毎年イベントが開催されます。 1,000 のより科学的な学会からの支援を受けたアジア および 700 以上の オープン アクセスを発行ジャーナルには 50,000 人以上の著名人が掲載されており、科学者が編集委員として名高い

オープンアクセスジャーナルはより多くの読者と引用を獲得
700 ジャーナル 15,000,000 人の読者 各ジャーナルは 25,000 人以上の読者を獲得

抽象的な

Synthesis and Characterization of a New Solution to Remove Plugging During Water Flooding: Study Case, Platform B of Bohai Oilfield.

Moussa Z. Salim, Kang Wanli, Hongbin Yang, Chao Chen, Xiaoyu Hou, K. Shola, Yuxi Li, Ming Lu

Formation plugging has occurred during water flooding process on B platform of Bohai oilfield, leading to an increase of injection pressures as well as the injected water volume due to the reduction in water layer adsorption within the formation. To overcome these issues, the present work intend to investigate the causes of such plugging, analyze the plugging sample, develop a new removal formula composed of surfactants and weak acids with ability of dissolving the plug, then characterize the solution and test its performances. SEM and XRD analysis were used to characterize structure and composition in elements of the plugging scale; the new developed removal solution did not contain strong acids, as they have been proved hazardous during the unplugging process for injection system. The new solution was found to dissolve up to 72% of the plug, with 2.12% corrosion rate. The solution was compatible with formation and injected waters, decreased the injection pressure system by 0.426MPa within 3PV of injection volume in a sand pack flooding experiment and has an acceptable pH of 5.8. A suitable removal solution for the plugging problems that the oilfield is facing.

免責事項: この要約は人工知能ツールを使用して翻訳されており、まだレビューまたは確認されていません。